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Don't let this happen to you.......
Just looking through old pics on my comp to clean up my desktop, and came accross these from an old customer who blew their motor drifting....
http://img.photobucket.com/albums/v2...eredpiston.jpg http://img.photobucket.com/albums/v2...nce/badrod.jpg http://img.photobucket.com/albums/v2...adrodblock.jpg http://img.photobucket.com/albums/v2...blockclose.jpg just thought i'd share... |
Originally Posted by Tony@Performance
Just looking through old pics on my comp to clean up my desktop, and came accross these from an old customer who blew their motor drifting....
http://img.photobucket.com/albums/v2...eredpiston.jpg http://img.photobucket.com/albums/v2...nce/badrod.jpg http://img.photobucket.com/albums/v2...adrodblock.jpg http://img.photobucket.com/albums/v2...blockclose.jpg just thought i'd share... |
this car was NA, only simple bolt ons. nothing major done at all, and routine service
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Originally Posted by Tony@Performance
this car was NA, only simple bolt ons. nothing major done at all, and routine service
Fred..:( |
bounching off the rev limiter way too many times...
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probably didn't but did warranty cover it?
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Originally Posted by palmerwmd
How could this have happened?
Fred..:( |
Originally Posted by Z2000Maximaguy
Oil does not lube properly when the car experiences sideways g-force over long periods of time. The stock oil system depends on gravity. Correct me if I'm wrong, this is my take on it.
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Wow the guts are all over the place.
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How could simple bolt on cause that. I actually read of someone else here on the board in Miami whos motor blew and No FI was in his car just bolt ons. How to avoid that then?
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I think the point is DRIFTING caused the failure (misuse)
NOT mods. In fact if he HAD some oil system mods, he probably would've been fine in my conjecture. |
Originally Posted by Z2000Maximaguy
I think the point is DRIFTING caused the failure (misuse)
NOT mods. In fact if he HAD some oil system mods, he probably would've been fine in my conjecture. |
Nice Z abortion photos
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quite possibly oil starvation? thats a shame....
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OUCH!!! looks like the 3.0L we took out of an N/A Z32 last year. He had been drifting too and we were of the opinion that it was oil starvation. He bought a new core, rebuilt the engine, added a higher volume/higher pressure oil pump and put a windage tray in the oil pan. Seems to be working as he's back at it again. He also does some track time.
We also wondered if he didn't over rev it a few times in the past. In any event, defecation occurs, don't it? |
I need to make something clear in this thread...
modifications did not cause this... |
Originally Posted by Jason@Performance
I need to make something clear in this thread...
modifications did not cause this... |
holy crap, thats a damn shame
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perhaps just a failure of the oil pump?
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how did drifting cause this??
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