Uncontrollable boost...Mystery of the ages
#41
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In reviewing the installation instructions (page 19/20), it indicates that there is supposed to be a gasket between the dump tube and the downpipe flange. I guess now a) I know where the 2nd gasket on the wastegate came from (the one that is NOT supposed to be there), and b) I know why I have an exhaust leak between the dump tube and the downpipe.
I'd still love to know how this could cause overboosting though....
I'd still love to know how this could cause overboosting though....
#42
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Originally Posted by disturbed2483
i though the same thing but its do-able but only out of the car, as crazy or stupid this may sound you can actually attach the dump tube to the down pipe out of the car and put it in the car as one whole piece but it must be done from the top, believe me its possible thats how I did it it just took some tlc. if you have any questions let me know.
#43
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Originally Posted by kcobean
I'm going to guess that you did this with the turbo itself out of the car? I was hoping to avoid having to yank the turbo out to get to these bolts, but it looks like I might have to, especially since the gasket that was supposed to be installed at the top of the dump tube was installed on the input port of the wastegate instead.
#44
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just curious, i think i read most of the posts till now, but have you tried simply taking the boost controller out of the picture and venting the top of the wastegate to atmoshpere. it would eliminate alot of possibilities if it then only let you build the 5psi of the spring in there.
#45
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Originally Posted by overZealous1
just curious, i think i read most of the posts till now, but have you tried simply taking the boost controller out of the picture and venting the top of the wastegate to atmoshpere. it would eliminate alot of possibilities if it then only let you build the 5psi of the spring in there.
This is all kind of coming up now because Sharif commented after tuning the car that he thought something might be wrong with the wastegate due to the high boost, and I finally got around to getting a new gate from Turbonetics, thinking that this would solve the problem. But apparently not.
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Well it appears the weirdness never ends. I still don't see how the wastegate leaking out from the dump tube could do this either but at this point I guess we just need to eliminate every possiblity...
#49
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Originally Posted by huducks
hey kelly just curious... but whats the highest boost u've seen out of the car so far? not that u would want to find out the hard way.
#50
Originally Posted by kcobean
The highest I've seen is 14 PSI, but that was just briefly and I had one eye on the gauge and one on the road. It's amazing how fast the boost builds once you hit around 4K rpm.
#51
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The problem w/ the increased boost level lies w/ the problem that not enough exhaust gas is being bypassed around the turbine. (duh).
Check the valve and seat of the w/g. Without the spring in the gate the valve should move freely. Could be a little sticky or not opening fully. That would cause the turbine pressure to rise.
Have you tried replacing the gate assembly completely? Not just the spring. Try swapping it out w/ another know working gate and see what happens.
Ok just read where you got a new gate from T-netics. Try one from a known working car. Chances are slim but it might have been a bad gate as well. Quality isn't exactly #1 w/ their products.
Check the valve and seat of the w/g. Without the spring in the gate the valve should move freely. Could be a little sticky or not opening fully. That would cause the turbine pressure to rise.
Have you tried replacing the gate assembly completely? Not just the spring. Try swapping it out w/ another know working gate and see what happens.
Ok just read where you got a new gate from T-netics. Try one from a known working car. Chances are slim but it might have been a bad gate as well. Quality isn't exactly #1 w/ their products.
Last edited by UnderPressure; 12-05-2005 at 02:30 PM.
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Originally Posted by UnderPressure
The problem w/ the increased boost level lies w/ the problem that not enough exhaust gas is being bypassed around the turbine. (duh).
Check the valve and seat of the w/g. Without the spring in the gate the valve should move freely. Could be a little sticky or not opening fully. That would cause the turbine pressure to rise.
Have you tried replacing the gate assembly completely? Not just the spring. Try swapping it out w/ another know working gate and see what happens.
Check the valve and seat of the w/g. Without the spring in the gate the valve should move freely. Could be a little sticky or not opening fully. That would cause the turbine pressure to rise.
Have you tried replacing the gate assembly completely? Not just the spring. Try swapping it out w/ another know working gate and see what happens.
#53
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Flow from the gate would be the only other possible cause. When the gate is off the tube, check to make sure the port into the exhaust is completely unobstructed. Hole could have been cut to small.
Edited my previous post once I finished reading the reast of the thread. Teach me to jump to conclusions.
Also check the hole size on the return to downpipe tube. The w/g could be fully opening but the hole back into the exhaust might be the size of a coffee stirrer.
Edited my previous post once I finished reading the reast of the thread. Teach me to jump to conclusions.
Also check the hole size on the return to downpipe tube. The w/g could be fully opening but the hole back into the exhaust might be the size of a coffee stirrer.
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Originally Posted by UnderPressure
Flow from the gate would be the only other possible cause. When the gate is off the tube, check to make sure the port into the exhaust is completely unobstructed. Hole could have been cut to small.
Edited my previous post once I finished reading the reast of the thread. Teach me to jump to conclusions.
Edited my previous post once I finished reading the reast of the thread. Teach me to jump to conclusions.
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It has to be an issue w/ the wastegate or the related systems. I'm leaning more and more towards the dumptube issue. The downpipe/exhaust can flow sufficent amount of exhaust gas to regulate turbine speed. What seems to be happening is the w/g is trying to bypass the exhaust gases but is unsuccessful. If the problem doesn't lie in the w/g itself it must be post-w/g a simple test would be to remove the w/g dump return and see if the car hold low boost. If not, then it's time to start looking @ w/g placement vs. exhaust back pressure.
#57
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If I was looking at this problem in a vaccum, then one could probably point to insufficent wastegate flow...ie...the gate is too small to flow enough exhuast to keep the pressure at the preset level.
But becuase there have been so many successful installs, it's hard to point the finger at the wastegate, especially now that Kelly has swapped it for a brand new one.
But becuase there have been so many successful installs, it's hard to point the finger at the wastegate, especially now that Kelly has swapped it for a brand new one.
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Off the wall but could the gas be flowing in such a way to create some kind of fluid dynamics effect (vortex, eddy or whatever) at the wastegate which is restricting the flow through it - so it opens but can't flow (vent) correctly.
And maybe the freer flowing (faster flowing?) exhaust setup could contribute to the above effect.
Told you it was off the wall and no idea how to verify LOL
And maybe the freer flowing (faster flowing?) exhaust setup could contribute to the above effect.
Told you it was off the wall and no idea how to verify LOL
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Originally Posted by prescience
Off the wall but could the gas be flowing in such a way to create some kind of fluid dynamics effect (vortex, eddy or whatever) at the wastegate which is restricting the flow through it - so it opens but can't flow (vent) correctly.
And maybe the freer flowing (faster flowing?) exhaust setup could contribute to the above effect.
Told you it was off the wall and no idea how to verify LOL
And maybe the freer flowing (faster flowing?) exhaust setup could contribute to the above effect.
Told you it was off the wall and no idea how to verify LOL
Well that's actually not that far off the wall. I think the problem is going to be much simpler and found as a partial blocked w/g feed or dump tube return.
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Originally Posted by MIAPLAYA
My concern is more then maybe they are flowing SOO much better with these exhausts that the dump tube just can't route enough exhaust gas past the turbine. I know its hard to believe thats it as I don't even believe it myself to the fullest but two of the three have the SAME setup, modified Greddy true duals and the other has the Topspeed Pro-1 which apparentely flows pretty damn well. The one thing to note is that the two that are running the modified Greddy true dual are not only getting 11+ PSI but they are running in the 9s AFR which makes ZERO sense. The injectors are at roughly 100% duty cycle by 10.5 PSI and I know at least in kcobeans case the fuel pressure is exactly like mine.
It would be hard to believe that the dump tube is blocked in some other way too. I mean what would be in there to block it, a cat?
I think there is enough info here and diagnostics that have been suggested that Kelly at least has some things to try. When he has some answers to these things I think he will be able to resolve the issue. Might take a long day at a good shop to try it all.