Bad Night, DEATH, The END, she's done. BOOM! 20+ psi error!
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Bad Night, DEATH, The END, she's done. BOOM! 20+ psi error!
This happened last night at the track.
Here is the VIDEO http://www.youtube.com/watch?v=HZr_LoNoGw0
now shes parked, and will be parked for a bit.
Here is the VIDEO http://www.youtube.com/watch?v=HZr_LoNoGw0
now shes parked, and will be parked for a bit.
Last edited by ipcheck; 11-29-2006 at 04:28 AM.
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well, temperature is low here these days, like 39-45, i had my boost controller off, and she just overboosted. PERIOD. gay right? Turbonetics relocation pipe not installed...
=(
=(
#6
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You had to know that without the relocation pipe installed this was to be your destiny.
Live and learn..... The point is to learn from others who have gone before you. This overboost issue has been known for over a year now. Some people have to learn the hard way.
Now build a motor and sell the TN kit for a Greddy TT like everyone else has. I'm counting the days til that's posted.
Sucks anyway... I feel for you. Been there. First the bumper crushed by your sister and now this!!
JET
Live and learn..... The point is to learn from others who have gone before you. This overboost issue has been known for over a year now. Some people have to learn the hard way.
Now build a motor and sell the TN kit for a Greddy TT like everyone else has. I'm counting the days til that's posted.
Sucks anyway... I feel for you. Been there. First the bumper crushed by your sister and now this!!
JET
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ipcheck - Sorry bro for the loss of the motor, but you can't blame this on not having the relocation pipe. You have a totally custom wastegate setup so this isn't the problem with the factory kit. Perhaps there was a problem with your custom setup? (I can't guess what because I don't know how it was configured)
Besides, I've never heard of anyone hitting to 20psi, overboost or not.
Either way, good luck on getting the rebuild.
Besides, I've never heard of anyone hitting to 20psi, overboost or not.
Either way, good luck on getting the rebuild.
Last edited by taurran; 11-22-2006 at 11:30 PM.
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Originally Posted by JETPILOT
You had to know that without the relocation pipe installed this was to be your destiny.
Live and learn..... The point is to learn from others who have gone before you. This overboost issue has been known for over a year now. Some people have to learn the hard way.
Now build a motor and sell the TN kit for a Greddy TT like everyone else has. I'm counting the days til that's posted.
Sucks anyway... I feel for you. Been there. First the bumper crushed by your sister and now this!!
JET
Live and learn..... The point is to learn from others who have gone before you. This overboost issue has been known for over a year now. Some people have to learn the hard way.
Now build a motor and sell the TN kit for a Greddy TT like everyone else has. I'm counting the days til that's posted.
Sucks anyway... I feel for you. Been there. First the bumper crushed by your sister and now this!!
JET
Get the whole story, Jet. He had a custom wastegate setup (neither a stage 1 setup or a turbonetics wastegate relocation)
Thanks for jumping on the turbonetics hating bandwagon, again...
Last edited by taurran; 11-22-2006 at 11:35 PM.
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Originally Posted by JETPILOT
THIS LOOKS LIKE AN EVOLUTION TO ME MOUNTED IN THE OE LOCATION.... Maybe you should get your story straight!
JET
JET
I'm going to wait for him to respond before we go any further.
He told me he had fabbed up a custom wastegate mount about 1-2 months ago (Since April). I don't believe this is the traditional "overboost" problem unless this was simply not true. In any sense, the "overboost" issue alone would not cause boost to spike to 20+psi. Cold air or not, that's just a rediculous amount of boost that would be indicative of an inoperable wastegate.
He also told me he had been running the car at 12psi without boost control this week and I advised against it since he would theoretically be out of fuel. I wouldn't have even run the car in that stage, but he said it felt solid.
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Originally Posted by JETPILOT
His post back from April talking about overboosting.....
https://my350z.com/forum/showpost.ph...52&postcount=1
JET
https://my350z.com/forum/showpost.ph...52&postcount=1
JET
You still don't have the full story on that issue. He was overboosting in that case due to the flex (ribbed) dump tube he had installed that was causing such backpressure that the wastegate wasnt opening. He replaced it with a smooth pipe and the overboost problem went away.
Meaning - that "overboost" problem you're referring to (due to a modified wastegate) was since FIXED::
https://my350z.com/forum/forced-induction/181920-installed-atmosphere-dump-huge-problem-big-time-overboost-read.html
Please refine your search skills before trying to own me again, thanks.
Last edited by taurran; 11-23-2006 at 01:55 AM.
#18
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8 psi spike is crazy.... i think something else might be a factor here.
i really dont understand why many people are pushing their stock motors and running boost controllers on the TN kit, i mean the tq levels are already high and i am crazy about pushing the limits.
sorry bout your motor man, good luck with the rebuild, if you near florida area, hit me up and i will see what i can do for you...
i really dont understand why many people are pushing their stock motors and running boost controllers on the TN kit, i mean the tq levels are already high and i am crazy about pushing the limits.
sorry bout your motor man, good luck with the rebuild, if you near florida area, hit me up and i will see what i can do for you...