When you click on links to various merchants on this site and make a purchase, this can result in this site earning a commission. Affiliate programs and affiliations include, but are not limited to, the eBay Partner Network.
check your throttle body. I know a friend of mine with a g37 had the same issue but not boosted. His had the TB F'ed. It was replaced. I have no idea if it could be the same issue, but Ijust trying to give in some feedback through prevues experience.
Well, the ground electrode of that sparkplug broke off and a bit of the insulator looks like it melted… swapped the plugs and it’s the same. I can’t post the log here, the file’s too big, could I shoot you an email if you wouldn’t mind taking a look at it?
Yeah, the tune hasn't been touched, the car just randomly started having an AFR in the 9's, I just drove it home from work and then to Intense, after that we pulled the plugs and found the plug in cylinder #2 broke. No misfire codes or anything.
Yeah, I’m really hoping that spark plug didn’t do any damage… I’ve got just over 2k miles on this motor… I think I’m going to try and swap the MAF sensor out tomorrow and iA the leak down test turns out good I’ll have the car towed down to ProEFI later this week.
is that spark plug broke for sure or melted? its one or the other for sure. im suprised the compression test went good, my guess is that remaining piece of grounding strap is whats causing the problem. did something happen with the car when you first got the codes/bad running issues?
So, I went down to Intense last night and got a bit of good news, the car passed the leak down test. Mechanically everything’s sound, the compression test results from last week were solid as well. I’m going to try and pull the injectors and check them next, after that the car’s going to ProEFI as a last resort.