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11.38 @ 119.32 MPH New RECORD 9/27

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Old Sep 29, 2003 | 09:55 AM
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Default 11.38 @ 119.32 MPH New RECORD 9/27

375 Shot of NOS and BOOM

Well the day started off great. The Performance Motorsport inc. team minus me arrived in PA at Maple Grove Raceway for some drag racing.

First Run

6:03 PM

R/T - .145
60' - 1.550
330- 4.690
1/8 - 7.286
MPH- 95.83
1000- 9.495
1/4 - 11.386
MPH - 119.32

VIDEO COMING I PROMISE

andrew will contribute to the rest of this thread later in the day.

we had NX problems and changed the NOS system, we has the best 60 foot ever 1.20 good for a 10.5 or 10.6 run but at 300 feet the engine blew... more VIDEO coming of that too...

Why ...ask andrew... what was the week link..again info comming,

For now enjoy the pics of the Motor and we will be back this weekend at NJ raceway Park running the old set-up...

more later...

Congrats Andrew.... 11.38 NEW RECORD for the Fastest 350Z 1/4 mile car in the world
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Old Sep 29, 2003 | 10:07 AM
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You guys are friggin' nutz running that big of a shot...with that said, congrats on the outstanding times!!!
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Old Sep 29, 2003 | 10:10 AM
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Man, what a mess. Any idea yet what failed first?
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Old Sep 29, 2003 | 10:13 AM
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Default YUP

Originally posted by teh215
Man, what a mess. Any idea yet what failed first?
andrew will join this thread later tonight to discuss what failed, and what it felt like in the car...
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Old Sep 29, 2003 | 10:31 AM
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Wow,

That's even more impressive than Ravas's "Holy Piston."

Can't wait to hear what happened.

-D'oh!
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Old Sep 29, 2003 | 11:02 AM
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375 shot....Wow
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Old Sep 29, 2003 | 11:31 AM
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That engine is Toast!!!! This is why I will never run a 375 HP shot !!! So what is the limit of the engine? Did you lean out or break stuff?
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Old Sep 29, 2003 | 12:23 PM
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OMG YOUR CRAZY!!! 375!!!
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Old Sep 29, 2003 | 01:16 PM
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Default VIDEO IS UP

check out the video .....

http://www.theexperience.com/video.p...=3f788cf314024
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Old Sep 29, 2003 | 01:19 PM
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NICE WORK!!


DAMN THAT SERVER SUCKS!! SLOW DOWNLOAD

Last edited by Wicked4u2c; Sep 29, 2003 at 01:26 PM.
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Old Sep 29, 2003 | 01:22 PM
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PLEASE DOWNLOAD to YOUR System do not just Click and Play...

Thanks...to JT for the quick turnaround time on the Video..
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Old Sep 29, 2003 | 03:45 PM
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Default Thanks- Great Video

Thanks for taking the time to put the video on display. Can't wait to hear the specifics on what broke & your opinion on what's the limit of N20 !!
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Old Sep 29, 2003 | 04:45 PM
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So would it be safe to say this motor can handle close to 500-600 w/o touching the internals?
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Old Sep 29, 2003 | 05:15 PM
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Wholly Shiot! Can I have your cat pipes? J/k
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Old Sep 29, 2003 | 06:59 PM
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hey everyone this is Andrew Rubio from Performance Motorsport.
first things first the things that did work:

got the full length headers from XERD. a very nice product that fit extremely well and actually kept the engine compartment noticeably cooler.

got the nismo cams in time also. a nice slighty lopey idle and a definite increase in response althouth a chore to put in.

while we were putting in the cams we decided to freshen the engine and put in new main and connecting rod bearings and new piston rings. but we left all other components stock; ie. pistons, con-rods, crankshaft, heads.
we also upped the shot on the direct port system to a 300 knowing that the engine could at least take that much from previous experience since we has a combined shot of 300 between both stages.

finally the runs.

first run off the truck was the 11.3 at 119. second run was an 11.4 at 118 but then we began to have problems with the nitrous controller. we're still trying to isloate them but as yet have been unable to ascertain the cause of the problem. we ran maybe 6 more runs with the nitrous cutting on and off the whole run and we were still running high 12. this was all without the 2nd stage by the way.

finally on sunday still not able to fix the problem with the controller we threw in a spare relay we had with us and wired the direct port system to come on with the button we used for the 2nd stage. so that meant that the full 375 shot would come on instantly. burnout, staged, light went green and you guys saw the video so u know what happened next. it launched like a saturn V rocket and had a combo of clutch and tire slip all through 2nd gear and when i looked down the tack said 7800 hehe. so i shifted into third, it hooked up finally and boom. i heard and felt something go clunk a bunch of times in the engine, followed shortly by a pop and the hood jumped about 6 or 8 inches up as the nitrous caused it to backfire pretty seriously. i pulled off to the side of the track figured out i wasn't really burnin and waited for the track guys to show up.

now for what failed,

now i know everyone says that the rods are the weak point in the VQ and in forced induction application that may very well be the case. but in a nitrous only application like we're running it's most definitely the pistons. 5 of the 6 pistons we broken into pieces, some large some small, and once the pistons broke i think u can figure out what happened next with the con rods. otherwise the con rods or what was left of them still spun on the crank and the crunk still spun in the mains. none of the main bearings pulled, the bolts were still tourqued correctly and the main bearings were so good we're keeping them as spares.

as to what it can take.

from our experience the engine is very tough and can take a 300 shot either staged or direct port. the other thing is that even though we weren't really using the progressive on the controller it still softenend the hit a little bit which seems to make it hold together. now im not saying that if u run a 300 shot on a street car it's not gonna break. but for a weekend or track application she seems like she can take it.

now for my last comment.
i know there are alot of you who have been following and supporting us here on this forum and to all of you i would like to say thank you, your support is much appreciated. what happened happens when you push to be faster and be number one. it's what racing is all about and when you are on the ragged edge sometimes you end up over it and something like this happens. it sucks we lost an engine but hopefully now you all may use this to your advantage and apply it to your own cars and not say i told you so.

i think that's it, if there's anything else let me know and i'll do the best i can.

thanks again
Andrew Rubio
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Old Sep 29, 2003 | 08:16 PM
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Andrew- thanks for the update. Sorry to hear about the engine. At least you guys are pushing the upper limits of the engine and sharing with the community which I'm sure everyone appreciates. Congrats on the time and I'm sure you guys will be back at the track in no time.
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Old Sep 29, 2003 | 08:34 PM
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That was an awesome 11.38 run guys. Hats off to your accomplishment and your hard work.
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Old Sep 29, 2003 | 09:11 PM
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Andrew, thanks for the great description.

So one thing I think I understand from this is that the crank is very tough as well? As in, it sounds like it can easily take using undamped UR pulleys in place of the stock damper without too much risk of breaking the crank.

Hope you guys can get another engine together without too much trouble!
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Old Sep 30, 2003 | 05:40 AM
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Amazing. Congrats guys.

Can you post all your mods again please?

Thanks.
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Old Sep 30, 2003 | 05:43 AM
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Originally posted by 99AllTurbo
Amazing. Congrats guys.

Can you post all your mods again please?

Thanks.
Injen - CAI
XERD - Header
Tein - EDFC
NISMO- Cams
NX - Custom System
Cobra - Racing Seat
Weld - Racing Wheels
Mickey T - Drag Slicks
Line Locks
Recordable Tach
NOS Controler System
Bosch - Spark Plugs
UR - Pulley and Clutch and Flywheel

Last edited by bluefish; Sep 30, 2003 at 05:52 AM.
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