Z Down.. Read to help diagnose...
Compression test wouldnt hurt. even if it's not the problem it's good to know what you're its at anyways
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sorry for delay in updates. I really have not had time to work on my own car. Only update i have is that I switched out the ecu with another 04.5 auto z ecu and flashed my rom on it. Still has the same missing cylinders. I will be burning the midnight oils tonight working on it along with tomorrow. Im either going to figure it out or part out.
Sounds like a wiring fault. Not sure why those wires you posted were melted like that - probably should look into all the harnesses.
Last edited by rcdash; Jul 11, 2011 at 11:18 AM.
sorry for delay in updates. I really have not had time to work on my own car. Only update i have is that i switched out the ecu with another 04.5 auto z ecu and flashed my rom on it. Still has the same missing cylinders. I will be burning the midnight oils tonight working on it along with tomorrow. Im either going to figure it out or part out.
Last edited by nismonian; Jul 11, 2011 at 12:22 PM.
The wires were not melted. Sorry for the pic it was done with a Ifail. The harness was pinched and smooched when a certain shop locally here ( last ones to ever touch my car besides me ever again ). So the wires are actually gashed. I am going to rip the whole harness out today and do a compression test along with a leak down. Ill take pics if I find anything.
Ok so finally got around to work on z. Finally did a compression test. Bad news. Cylinder #2 has zero compression...... So started the process of pulling the motor last night. I will update again once i get a chance to take a look.
Wow it has been a while since i updated this. Sorry for those who were following. After removing the turbo manifold I could see it was a dropped exhaust valve. After removing the head It was confirmed. No contact was made and pistons looked perfect. Also, head gasket was still great. ( HR btw ). Removed the valve and going to re install a new one. then put it back together and move fwd.
Yeah i was pretty excited to open her up and not see a cracked piston.
Cause?
I would imagine over revving the motor. I turn it to about 7200. Its has Ferrea springs and retainers w/ stock valves. Cam is a Tomei 264 cams, but im not expert so who knows.
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